
SDR 510023944 | Gulfstream 500S Wing miscellaneous structure—wing strap cracked. During AD/AC/93 Inspection stage 1, R/H lower wing strap found with 3 cracks, as confirmed by FPI as well as eddy current. Requirement 2 of AD/AC/93 was then carried out with nil defects found. During AD/AC/93 requirement 3, R/H upper frame at F.S. 100.00 was found cracked , as confirmed by visual inspection. Confirmation by NDT not required. P/No: 1700368. TSN: 26437 hours

SDR 510023941 | Beech 76 Landing gear actuator—cylinder separated. During flight, pilot observed some mechanical issue with the under carriage . After verifying gear down through fly by inspection , safe landing was made. During ground checks it was learned that NLG actuating cylinder has separated causing the pressure to be released from the system thus causing the gear to gravity extend. Service data search indicated failed component has good reliability. Maintenance removed the Actuator and after inspection advised that the Cylinder failure was a clean break with no obvious pre-existing defect. A new Actuator was fitted. Gear swings carried out with nil defects and the aircraft returned to service. P/No: A2178A.

SDR 510023941 | Beech 76 Landing gear actuator—cylinder separated. During flight, pilot observed some mechanical issue with the under carriage . After verifying gear down through fly by inspection , safe landing was made. During ground checks it was learned that NLG actuating cylinder has separated causing the pressure to be released from the system thus causing the gear to gravity extend. Service data search indicated failed component has good reliability. Maintenance removed the Actuator and after inspection advised that the Cylinder failure was a clean break with no obvious pre-existing defect. A new Actuator was fitted. Gear swings carried out with nil defects and the aircraft returned to service. P/No: A2178A.

SDR 510023876 | Bombardier DHC8-202 Passenger compartment lighting—lamp holder burnt. During pre flight checks, crew reported burning smell in cabin and around the radar console. Smell was traced to X2 burnt cabin sidewall fluoro tube holders. Affected tubes removed from holders and MEL applied. During the course of rectifications, suspect lamp holders were replaced. One was found badly burnt where as the other was cracked. System tested serviceable. P/No: BV033021148BV033001248.

SDR 510023849 | Lycoming IO540AE1A5 Fuel control/reciprocating engines—rod end separated. Throttle forward rod end at FCU found separated. Removal of the cover revealed that the swage had failed. The R44 IPC shows an A141-17 large area washer, found not installed. Other R44 II aircraft of a similar age also did not have this washer installed. Installation of this washer would have prevented a complete disconnection of the rod after the failure. OEM notified. P/No: A1273.

SDR 510023811 | Gippsland Aeronautics GA8 Main landing gear strut/axle/truck—axle cracked. While doing an 100 hourly inspection of undercarriage axle assemblies, a crack was noticed in the welded transition area. Paint was removed and with the help of 10X magnifying glass, cracks on both LH and RH axle assemblies were noticed. Dye penetrant inspection confirmed the flaw. Four similar defects reported. P/No: GA8321023011. TSN: 8628 hours

SDR 510023811 | Gippsland Aeronautics GA8 Main landing gear strut/axle/truck—axle cracked. While doing an 100 hourly inspection of undercarriage axle assemblies, a crack was noticed in the welded transition area. Paint was removed and with the help of 10X magnifying glass, cracks on both LH and RH axle assemblies were noticed. Dye penetrant inspection confirmed the flaw. Four similar defects reported. P/No: GA8321023011. TSN: 8628 hours

SDR 510023810 | Gippsland Aeronautics GA8 Horizontal stabilizer spar/rib—stabilizer cracked. During inspection against mandatory service bulletin SB-GA8-2002-02, crack found in rear spar of horizontal stabilizer. Rectification carried out IAW mandatory service bulletin SB-GA8-2009-59. P/No: GA8551011011.

SDR 510023793 | VICTA 115 Wing spar corroded. While the wing was removed for AD/VAT/28 compliance, corrosion was discovered in the main spar web at the L/H forward wing attachment point.This area is not specifically mentioned for inspection for corrosion in AD. Inspection is only possible after removing the fuel tank.

SDR 510023766 | Champion Spark Plug Co 4373 distributor gear failed. During an engine run, when magneto (4373) was selected, engine ran rough and backfired. The magneto was replaced with a serviceable unit and ground run serviceable. Within the suspect magneto, evidence of burning was found around the distributor assembly. Going forward, distributor and gear assembly was removed and opened for inspection. Inside the cap, was evidence of burning and copper deposits. The distributor gear (K3008) was found to have a loose and damaged finger that showed signs of electrical burning. The gear also had signs of burning. The loose finger combined with the carbon-copper deposits in the cap would have cause the HT to randomly track causing the rough running engine and back firing.The magneto will have a new distributor and gear assembly fitted. The problem with the distributor gears is known with Lycoming SB622 and Slick SB1-15 addressing the issue. P/No: K3008. TSN: 658 hours TSO: 658 hours

SDR 510023756 | Cessna 172P Crew station equipment system—repair kit incorrect fit. Secondary seat stop anchor point incorrectly installed with hole drilled to inaccurate dimensions. P/No: SK210174AINSTALLATION J.

SDR 510023724 | Gulfstream 690A Electrical power wiring—wire loose wiring. While undergoing major avionics upgrade, following discrepancies were observed. 1. CB’s terminals stripped of thread and blue tack used to secure screws. 2. CB panel dangerously wired (over time) with some wiring at loose ends and looms not secured. 3. Instrument panel as above – looms not secured and wiring found with loose ends and not secured. All wiring repaired and CB’s replaced.

SDR 510023724 | Gulfstream 690A Electrical power wiring—wire loose wiring. While undergoing major avionics upgrade, following discrepancies were observed. 1. CB’s terminals stripped of thread and blue tack used to secure screws. 2. CB panel dangerously wired (over time) with some wiring at loose ends and looms not secured. 3. Instrument panel as above – looms not secured and wiring found with loose ends and not secured. All wiring repaired and CB’s replaced.