
DR 611649231 | ATA 8550 RECIPROCATING ENGINE INTERNAL OIL SYSTEM—BAFFLE DAMAGED. During inspections, engine sump baffle was found damaged. Part replaced.

DR 611649230 | BOEING 717 200—ATA 1200 SERVICING AIRCRAFT GROUND DAMAGE. Extreme weather initiated ground equipment movement caused damage to the aircraft.

DR 611649230 | BOEING 717 200—ATA 1200 SERVICING AIRCRAFT GROUND DAMAGE. Extreme weather initiated ground equipment movement caused damage to the aircraft.

DR 611649166 | BOEING 717 200—ATA 5544 RUDDER, MISCELLANEOUS STRUCTURE WASHER LOOSE. Following multiple reports of cracked brackets and rods holding heat exchanger and ACMs, Engineering discovered excessive play within the aft Rudder mechanism. Apparent lack of positive locking found at this installation. Boeing confirmed this finding and provided relevant drawing to enable this installation to be adjusted into the correct configuration. Aft Rudder mechanism was re-assembled with positive locking achieved through star washer. Post maintenance check flight has been conducted with nil discrepancies noted.

DR 611649156 | CESSNA 208 B—ATA 2730 ELEVATOR CONTROL SYSTEM TOOL STUCK. During flight control rigging check, pilot checked full and free movement of all flight controls. Very slight friction or binding of the elevator control was identified. The issue was discussed with the LAME who investigated further and discovered an object wedged between the control column shroud and the control column attaching cables. The shroud was removed and a screw driver was found.

DR 611649156 | CESSNA 208 B—ATA 2730 ELEVATOR CONTROL SYSTEM TOOL STUCK. During flight control rigging check, pilot checked full and free movement of all flight controls. Very slight friction or binding of the elevator control was identified. The issue was discussed with the LAME who investigated further and discovered an object wedged between the control column shroud and the control column attaching cables. The shroud was removed and a screw driver was found.

DR 611649144 | SIKORSKY S92 A—ATA 6797 ROTORS FLIGHT CONTROL WIRING LOOM INCORRECT FIT. Pilot reported there was a restriction of the cyclic movement in the forward left quadrant. Engineering investigation found cyclic wiring loom prevented full throttle movement to the stop. Wiring loom rerouted to prevent restriction.

DR 611649144 | SIKORSKY S92 A—ATA 6797 ROTORS FLIGHT CONTROL WIRING LOOM INCORRECT FIT. Pilot reported there was a restriction of the cyclic movement in the forward left quadrant. Engineering investigation found cyclic wiring loom prevented full throttle movement to the stop. Wiring loom rerouted to prevent restriction.

DR 611649046 | EMBRAER EMB120 ER—ATA 2420 AC (ALTERNATING CURRENT) GENERATION SYSTEM FAN BROKEN. PAX and FA reported sparks coming from the LH exhaust. All engine indications were reported normal. LH Starter Gen Cooling Fan and Cooling Duct had come into contact with each other causing damage and sparks. It appears that part of one of the fan blades became detached which resulted in the damage. LH Starter Gen replaced with a serviceable item. Unserviceable part has been sent to approved repair station for repair.